Cracked stiffener plates, secondary highway bridge
Matter
County DOT requested root-cause analysis on three stiffener plates showing toe cracks at the fillet welds, discovered during a biennial inspection. The bridge had been in service eleven years. Original fabrication records were available but incomplete for the stiffener welds specifically.
Approach
Sectioned transverse through the crack plane on all three plates. Macro-etch with 10% ammonium persulfate. Hardness traverse across HAZ, 0.5mm step. Optical metallography at 200× and 500×.
Finding
Weld metal was sound. Base plate showed banded microstructure with coarse pearlite colonies aligned parallel to the rolling direction. Cracks initiated at weld toes where the banding intersected the HAZ. Not a weld defect — a base-plate susceptibility amplified by joint geometry. Recommended retrofit stiffeners be cut from normalized plate.
Outcome: retrofit specification revised. Matter did not go to dispute.